I have a 2025 6MT. CTS Catless downpipe, RK Titanium single exit exhaust, MST V2 Intake and Turbo Inlet, I also had issues with MHD Stage 2 93. I would sometimes go into limp mode after doing a pull. I switched to 91 and everything was running better. I always use Shell 93. Speaking of the CDV...
The vband connection from my downpipe to turbo keeps loosening. Every day I go out and can tighten it. Not sure why but I ordered a new vband gonna put it on. When installing do you guys put anything on the vband threads like antiseize? Or just tighten it with nothing on?
Yea the codes were all misfires. Car was driving and idling fine besides getting that notification after a pull. I changed spark plugs and car works great 👍🏼
Recently got dyno tuned. Car made 415WHP and 505TQ on 93. I have a CTS Catless Downpipe, MST V2 Intake, RK Titanium Single Exit Exhaust. Driving from work last night I did a pull and got this message. Car went into limp mode. What can be the issue?
i dont think so. and i mean in the cabin i smell some gas but thats to be expected going catless right? i just rotated the clamp and tightened it down. seems more closed maybe that might have been it
Could this be due to a leak? I’m not 100% positive I pushed the exhaust all the way into the downpipe. It wouldn’t budge anymore so idk it was in a good amount. And I don’t see any visible soot by any connections
Does this link work for you?
https://datazap.me/u/stasoulakisa/log-1762059601?log=0&data=3-16
I got in my car and drove home after work. The first 10 minutes everything was great worked like normal even hit 21+ psi. And then out of nowhere it went into almost a limp mode and can’t pass 9psi...