suptj
Well-Known Member
- First Name
- TJ
- Joined
- May 21, 2023
- Threads
- 11
- Messages
- 70
- Reaction score
- 34
- Location
- Arizona
- Website
- www.trackbuilt.co
- Car(s)
- A91
- Thread starter
- #1
Hi guys was hoping you guys could look through my logs, and possibly give me some advice with my timing issues.
I recently purchased my Supra, bought it used from dealer 26k miles.
Installed catless DP, CTS CP, Armaspeed intake, BM3 tune last week. BM3 Flex fuel kit is awaiting shipment.
Ran the stage 2 91 map, e25 blend to compensate for Arizona gas, timing was all over the place.
06/23 Log: https://www.bootmod3.net/log?id=6496615fc090c698801b910a
Changed plugs today, add more E, now on e30 blend. Made improvements but around 5500rpms, timing takes a dump.
06/27 New plugs
Log: https://www.bootmod3.net/log?id=649b3315ae729b7a51f951a4
I noticed in the logs I'm no longer hitting target boost and higher WGDC. So I thought possible boost leak?
I let the car cool down removed the CP, checked o-rings and reinstalled with T-bolt clamps at the coupler. Also decided to drop down to the stage 2 ACN 91 map, still no luck.
06/27 New clamps/reset adaptations Stage 2 ACN91
Log: https://www.bootmod3.net/log?id=649b7b9bc090c6af235501bf
I just ordered new OEM o-rings for the CP, those arrive in a week. I also ordered the parts to run a boost leak test.
Do you guys have any other ideas? I know the IAT's are high causing some correction (Arizona ~105F ambient temps), but the timing completely dropping off at 5500 has me stumped. Other guys with that have similar high WGDC issues still retain their timing while mine takes a dump.
Thanks in advance!
I recently purchased my Supra, bought it used from dealer 26k miles.
Installed catless DP, CTS CP, Armaspeed intake, BM3 tune last week. BM3 Flex fuel kit is awaiting shipment.
Ran the stage 2 91 map, e25 blend to compensate for Arizona gas, timing was all over the place.
06/23 Log: https://www.bootmod3.net/log?id=6496615fc090c698801b910a
Changed plugs today, add more E, now on e30 blend. Made improvements but around 5500rpms, timing takes a dump.
06/27 New plugs
Log: https://www.bootmod3.net/log?id=649b3315ae729b7a51f951a4
I noticed in the logs I'm no longer hitting target boost and higher WGDC. So I thought possible boost leak?
I let the car cool down removed the CP, checked o-rings and reinstalled with T-bolt clamps at the coupler. Also decided to drop down to the stage 2 ACN 91 map, still no luck.
06/27 New clamps/reset adaptations Stage 2 ACN91
Log: https://www.bootmod3.net/log?id=649b7b9bc090c6af235501bf
I just ordered new OEM o-rings for the CP, those arrive in a week. I also ordered the parts to run a boost leak test.
Do you guys have any other ideas? I know the IAT's are high causing some correction (Arizona ~105F ambient temps), but the timing completely dropping off at 5500 has me stumped. Other guys with that have similar high WGDC issues still retain their timing while mine takes a dump.
Thanks in advance!
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